The 'reversion' to petrol turned out
to be a major project. The first task was to determine what parts would
have been installed on the engine originally. I tried a variety of sources
before hitting on the idea of locating someone in the U.K. with a similar car.
I used an Internet based registry of Morgan owners and located three who met the
criteria. I sent emails to each of them and got a prompt response from one
- Mike Schofield in Lytham St. Annes. Mike has
a '90 4/4 and was immensely helpful. He sent me a number of photographs,
partially disassembling his car to take some of them. He went to the local
Ford agent and got a copy of the parts page for the fuel pump. And he sent
me a dimensioned drawing of his fuel tank. It turned out that the
particular carburetor used on that engine was one only available in Europe.
I was able to find a business in England that could supply the carburetor and
the fuel pump, so I was in business.
The next challenge was the fuel tank. I decided to have one
built locally so that I could 'duplicate' Mike's tank. Based on the
measurements, it had a capacity of about 17 gallons. I felt it would be
wise to ensure that it would fit into our Morgan, so I removed the spare wheel
and the panels beneath it to take some measurements. That was when I
discovered another major challenge. There is a wooden structure that
supports the spare wheel in Morgans as they come from the factory. They
have a wooden frame mounted on a steel chassis, so this was no surprise.
The surprise was that our car no longer had that structure. It had been
removed when the conversion to propane was done. So now I had to figure
out how to fabricate a replacement structure that could be mounted in the car
with the body on. The factory puts all that part together before mounting
the body panels. The good news was that the tank would fit. That
would give us wonderful cruising range.
I located a local company that could
build the fuel tank for me at less than half the cost of ordering one from
England. I created detailed plans for the tank from the drawing Mike had sent.
I went to a local firm to get the fittings for fuel feed and return. They were
able to locate a pressure relief/rollover check valve for me. For the filler
neck, I picked up a piece of muffler tail pipe. Part of this pipe was also
taken to a fellow who could fit it to the underside of the fuel cap to replace
the neck that had been cut off during the propane conversion. With all these
things in hand I ordered the tank.
Returning to the missing wooden
structure, I designed a replacement structure that could be installed with the
body on the car and picked up two pieces of Ash – a 1 x 8 x 72” piece that could
provide the two boards the fuel tank sits on and a 1 x 6 x 72” piece that could
be ripped to 1 ¾” wide pieces to build the spare wheel support frame.
I ripped the 1 x 8 to 7 ½” wide,
figuring that the extra 1” (the bottom of the tank is 14” wide) could be used as
a place to mount the fuel filter. Then I cut it into two pieces 36” long. The
original boards were only ½” thick, so I dado’d the ends of the new boards to
that thickness to avoid having the fuel tank sit too high. The holes where the
boards attach to the frame rails and where the tank attaches to the boards were
drilled once the boards were in place. The hole that provides access to the
drain plug was cut at that time also. At that point the tank boards were ready
to be treated with a wood preservative.
I learned that the metal Relief line on
the propane tank could be disconnected from the upper spare wheel well body
panel with no problem. Once that was done the upper panel could be removed.
That made design and measurement of the new support frame pieces much easier.
At that point I also removed the bolts holding the propane fill and vent
fittings in place. I found that 90° angled pieces of sheet metal had been
installed on both sides to make the rear body panel less flexible. They were
bolted to the inner fender walls and had holes through which the fuel caps were
attached. The one on the left (fill) side was 1/8” thick and the one on the
right side was 1/16” thick. I decided to retain them, but notched the corner
where one of the horizontal wood frame members would go.
I also found that the radio antenna had
the cable to the radio along side the mast. The antenna had been installed so
that the cable was between the inner fender wall and the mast. I turned the
antenna 180° to provide more clearance for the wood frame member that would
attach to the inner fender wall. That gave me about 5/8” clearance.
I had measured the depth from the rear
body panel to the removable panels at 1 3/8”. I could see where the
original wood frame side members had attached to the inner fender walls, and
determined that the original depth would have been about ¾” greater. I
decided to split the difference to ensure that the new frame would clear the top
of the tank. As you will see from the following
documentary, this was a sort of ‘Rube Goldberg’ project. I was having to devise
ways to establish positions and take measurements to try to make the new frame
as square as possible. It would not be perfect, but it would be good enough and
it would be adequately stout.
I measured the angle (crudely) made by
the rear body panel and the bumper impact absorber where it attached to the
inner fender wall. The plan was to cut that angle on the ends of the side
members of the wood frame to maximize the surface for mounting the horizontal
frame members. I cut the left side member first and verified that it fit as
planned before cutting the right side member. The next step was to determine
where to dado the undersides of those members so they would fit flush over the
pieces of sheet metal mentioned earlier. I held those pieces of sheet metal in
place and scribed a line around their edges on the inner fender wall. Then I
held the side members in place and marked the area to dado. I also marked the
right side member where it would have to be notched for the radio antenna.
There is a piece of wood that is part of
the car’s frame and runs across the back at the top of the rear body panel. I
measured 3 5/8” down from that piece as the place to position the upper
horizontal frame member. The lower member would be mounted as low as possible
but it would be higher than the original because of the bumper impact
absorbers. That produced a span of about 10” between the inner edges
of the upper and lower frame members.
The span between the vertical members
was dictated by the location of the rain hat for the propane tank. If the rain
hat was not reinstalled there would be a large hole in the upper removable body
panel. That span was 11”. That yielded an outer span of 14 ½”. The ¼”
aluminum plate that supports the removable body panels is 16” wide. It was to
be mounted to the vertical frame members with 4 countersunk flat-head bolts.
Before removing the propane tank I reattached the aluminum plate and measured
the placement of the holes where the wheel support is attached. After the new
frame was installed, the aluminum plate was positioned and the holes drilled to
attach it to the new frame.
Upper bolt holes in the side members
were the next order of business. I was able to use an existing 3/8” hole on the
left, but had to drill a new hole on the right. To get the side members
properly positioned I cut a 10” long by 2 3/8” wide piece of wood. This piece
was placed against the inner fender wall and up against the under side of the
rear body panel. The side member was then snugged up against this piece and
downward against the bumper impact absorber. This ensured that the depth was
uniform top to bottom and on both sides. Once the side members were drilled, I
secured them with bolts so that I could mark the ‘precise’ location of the upper
horizontal member.
I had a piece of wood that would just
rest on both side members and could just be inserted beneath the rear body
panel. I taped a small piece of cardboard to the left side member at the top of
the planned cut for the horizontal member. I then held the horizontal test
piece up against that cardboard and measured down from the piece of frame
mentioned two paragraphs up. When I was satisfied that the test piece was
properly positioned I marked the edge of the right side member with an Exacto
knife. A pencil mark would not have been sufficiently accurate. The side
pieces were then removed and I marked the edge of the left member with the
knife. I then measured down from the knife cuts to mark the position of the
bottom horizontal member. That, in turn, gave me the length of the vertical
members.
I cut the notches in the side members
and sanded them to fit the horizontal members into the notches. It was a lot of
detail work, but it paid. With the side members done I turned my attention to
the horizontal members. I first dado’d the inner ends to a width of 2”. Then I
took them to the car and measured the dimension by which they failed to mate.
Dividing this dimension in half (one half for each side), I trimmed the outer
ends and rechecked them in the car.
After sanding the surfaces of the dado
cuts I marked the positions of the vertical members. I made the dado cuts for
them and sanded the surfaces of the cuts. I then rechecked the length of the
vertical members (the distance between the extremes of the notches in the side
members). I cut the vertical members and made the dado cuts at the ends and
sanded them.
The frame was done. I still had to
treat the pieces with wood preservative. I had to drill holes and glue and
screw the pieces together, but that had to wait until the propane tank was out.
The first task was to put the side members back in place with their top bolts.
I was able to drill the holes for the bottom bolts and start assembling and
installing the frame. It was very gratifying that it had come together just as
I had envisioned it.
I had to be able to properly position
the aluminum plate, so I reattached it to the propane tank with the two large
bottom bolts. I then measured the distance between the center of the bottom
bolt hole where the spare wheel support bracket is attached and the inner fender
walls. It was 18 5/8” to both sides. I measured the top bolt hole and was
surprised to find 18 27/32” to the left and 18 13/32” to the right. I mounted
the spare wheel bracket and the spare and took a look. Sure enough, the spare
is closer by just a bit to the right side of the round opening in the rear body
panel.
As I sat sipping a glass of wine and
reflecting on the day’s work I had an idea for positioning the aluminum plate.
I took two slim pieces of wood cut to 24” long and measured 18 5/8” from one
end. I marked that point and drilled holes the size of the bolts that attach
the spare wheel bracket. I was then able to position the plate laterally with
ease. From there it was a snap to position it vertically before clamping it to
the frame and drilling the mounting holes.
All
woodpieces were cut out of 1” Ash that had an actual thickness of 13/16”. The
tank boards were 35 5/8” long. The ends were dado’d to ½” thick, which was the
thickness of the original factory boards. The dado cuts were 1 11/16” in from
the ends, which left 32 ½” of full thickness that sat between the frame rails.
The spare wheel support frame had two extra pieces that ran horizontally and
were glued and screwed to the under sides of the main horizontal members. Those
pieces were 35 ½” long. The main horizontal members were 19 5/8” long and had
dado cuts half their thickness and two inches wide to allow them to overlap in
the center. There were also dado cuts half their thickness and 1 ¾” wide to
accommodate the vertical members. Those cuts were 11” apart, which produced a
distance between the outer edges of the vertical members of 14 ½”. The vertical
members were 11 ¾” long and had dado cuts half their thickness and 1 ¾” long at
each end. The side members were 15 7/8” long on the top edge and 11 7/8” long
on the bottom. They were notched to allow the horizontal members to fit flush
with their upper edges. The notches were cut such that the distance between
their outer edges was 11 ¾”. That put them as close to the full width part of
the member as possible. Screw holes were pre-drilled and countersunk for the
flat-head brass wood screws. There were two holes at each point where a
horizontal member mounted to a side member. There were also two holes where the
left and right horizontal member overlapped. There was one hole where each end
of the vertical members notched into the horizontal members. There was an
additional hole 4” inboard from each of the vertical member holes. That made a
total of eight holes that had 1 ½” screws that went through the horizontal
members into the extra pieces that were meant to reinforce the structure. The
notch in the inside of the right side member was for the radio antenna.
The tank boards and pieces of the wooden frame that
supports the spare, and the frame as it would look once installed, with the
aluminum plate in place.
I got started early on removing the
propane hardware. The first step was to shut the valve to the line that feeds
the propane carb. Then I loosened the fuel line at the valve. There
was an escape of pressurized propane for a few seconds. Then I
disconnected the fuel line from the valve.
The propane hardware before removal
From there it was a simple matter to
remove the propane hardware from the engine compartment. The next step was to
remove the propane tank. Remove all eight bolts that secure the tank to the
steel plates and the plates to the chassis rails and the tank just rotates
forward and down. It was rather heavy, so it helped to have a jack under it. The
fuel line was then removed by pulling the upholstery away from the
passenger side and disconnecting the clamps.
The propane hardware had been removed in this photo
The left side member of the spare wheel
support frame had to be in place before the fuel cap with filler neck was
installed. It seemed as if the best way to deal with that was to glue and screw
the horizontal members to both side members early. Once the propane tank
was
removed I put the side member/horizontal member assemblies in place and
temporarily screwed them together. Then I drilled the lower holes through the
side members, the sheet metal and the inner fender walls. I double checked the
point 3 ½” forward of the rear chassis cross member. This would be the rearmost
point of the top of the fuel tank. I measured up from that point 11 ½” to
verify that the spare frame would clear the top of the tank. Then I completed
assembly of the spare frame.
In the afternoon I picked up the tank.
It was rather heavier than I had expected, because they built it from 12 gauge
steel rather than 14 gauge. It is much beefier than a stock tank. We found
that the tank boards could not be moved into place as is, so we cut 45 degree
angles off of opposite corners of the dado’d part of the boards. That did the
trick. There was no way to get the tank in place with a board already in, so we
lifted the tank up and held it high enough to move the boards in under it. I
had measured the spot where the hole would be needed for access to the drain
plug. Unfortunately, I didn’t have a jig saw handy, so the hole is rather
rough. What the hell, nobody looks under your car anyway. We had to position
the tank on the boards and mark all hole locations, then take everything back
out to drill the holes in the boards.
The new tank was a very solid affair
The bolts that secure the boards to the
chassis and the tank to the boards were put in from the bottom up. This way
there was minimum area to be buggered up by running over anything. I figured
out that if I slid the tank as far to one side as possible, I could just barely
get my hand in to put washers and nuts on the bolts that secure the boards to
the chassis. Once that was done I repositioned the tank and secured it. Being
rather slim really helped, as there is very little space along side the tank.
Finally, I marked and drilled the pilot holes and secured the additional straps
to the bottom of the tank boards. The tank was in and everything fit, albeit
rather snugly.
The new tank and wood frame in place
I had earlier put the wooden frame in
place and glued and screwed it together. You can only get so far out from
center to put screws into the frame from above. I drilled two additional holes
from below as far outboard as possible and put screws in the bottom horizontal
member. The frame is very stout and should easily support the spare. The
bottom horizontal member, with its extra board on the underside, almost rests on
the tank. We took two strips of neoprene and sprayed them with adhesive and put
them between the tank and the frame. This would help prevent squeaks.
As we went through all this we took time
to test the fuel tank sender unit. The fuel gauge didn't register.
As I
looked at the dash it was obvious that a different fuel gauge was installed during
the propane conversion. It looked like the other gauges until you noticed that
the bezel that secures it was much wider than the others. I sent an email
to see if I could get a replacement gauge.
Bill, the guy who has the expertise I
lack, installed the fuel lines. We put in solid steel lines from the tank
to the fuel pump, connected by short rubber hoses and clamps. The steel lines
run inside the passenger area, just as the propane line did. They were tucked
under the upholstery on the passenger’s side. We restapled and reglued the
upholstery. We had to remove the passenger’s seat to install the fuel lines.
I had cut the tank boards 1” wider than
the bottom of the tank. We mounted the fuel filter atop that 1” space. The
clamp that holds the fuel filter and the clamp that holds the fuel line in place
are screwed into the leading edge of the tank board. New holes were cut in the
firewall and the fuel lines pass through those holes (and grommets). The fuel
lines were secured with clamps as appropriate and were positioned so that they
wouldn’t suffer any interference from the suspension. Where wood was available we
used screws on the clamps. In other places the clamps were pop riveted. Bill is
enough of a perfectionist that the whole thing looked very professional.
The fuel pump and carburetor were then installed and plumbed. One of the
heater sized hoses came forward and was held in place under the choke. It
then angled down and connected to the fitting in the intake manifold. There
were also electrical wires to the two connections on the carburetor that
control the choke and idle. Those were strap tied to the section of heater
hose mentioned. There was an in-line fuse in those wires. The original PCV
system was retained. A hole was drilled in the bottom of the air filter
housing to provide a source of clean air for that system.
The new carb and fuel pump had been installed in this
photo
Meanwhile, as Bill was working on the
‘innards’, I was positioning the aluminum plate and drilling it to secure it to
the new wooden frame. I had previously measured the distances from the centers
of the spare wheel bracket holes to the inner fender walls and to the top and
bottom of the circular opening in the rear body panel. I held the plate in
place with C clamps just loose enough that it could be moved until it was
properly aligned. It was secured to the bottom horizontal frame member with wood
screws and to the vertical members with flat head bolts and nuts. The screws
and bolts were countersunk to permit the removable panels to sit flush to the
aluminum plate.
All the heater hose and the three
radiator hoses were replaced at the same time. The only section of original hose
was the
short one that connects to the water pump. The alternator drive belt and
the timing belt were replaced.
The conversion was complete. We refilled the radiator, emptied a five gallon gas can into the tank and fired her
up. The carb was adjusted and the idle set to 800 RPM. Everything worked
as it should, with operating temperature in the right area and the fan coming on
and shutting off properly. It was time to drive it. I took her down the road to
the gas station and pumped in another 12.2 gallons. That put capacity at just
over 17 gallons, which would yield a great cruising range. I drove back to
tell Bill about the capacity and report first impressions. As I pulled back in
and made a left turn, the guys noticed that I was leaving a trail. I hadn’t
realized that with the tank full, gasoline would slosh up through the pressure
relief valve. I had come off the top of the valve with a 90 degree fitting
and a hose that runs down and out by the right rear fender to keep fumes away
from the passenger area. I had to revise that fitting, but had it figured
out. I took her out onto the freeway and put my foot in it in second and
third gears. In third I could really feel the secondaries kick in. She really flew.
I was grinning ear to ear.
The solution to the problem with the
fuel tank vent was really quite simple. I picked up two T fittings and another 4
feet of hose. I turned the flare nut fitting about 180 degrees so it faced to
the left and slightly forward. I inserted one leg of a T about 5 inches from
the bottom. The opposite leg of the T had a section of hose that continued
upward and looped over. It was connected to the side of the second T. A short
piece of hose from the lower leg of the second T went back down and connected to
the side of the first T. A much longer piece of hose was connected to the top
leg of the upper T and went upward in a loop and then back down and out into the
right rear wheel well. If fuel sloshed out the valve and up the hose and
actually managed to make it over the first loop, it would drain back down the
hose that connects the two Ts and back into the tank. It would not make it
up the second loop.
The new plumbing for the pressure
relief valve
Having remounted the right side prop rod
bracket and fixed the fuel tank vent, I took her out for a mileage test run. I
drove over to Puyallup so I could see how she pulls up the 512 Puyallup hill.
She went up the hill in fifth and was actually able to accelerate. I pulled off
the freeway and went over to Costco to top off the tank. Then I set off on the
mileage test run. I drove back over to I5 and took I5 down to Rochester (exit
88) and then back up to Gravelly Lake Dr. (exit 124). On the way I was able to
accelerate up the Nisqually hill in fifth. Much of the run was at speeds from
65 to 80, with a brief spurt to 85. I got off I5 and pulled into a station and
topped off the tank again. I had averaged a little over 31 MPG (I used to get
about 23 MPG on propane). That would give me a cruising range of over 450
miles. So the conversion has yielded more power, much better mileage, and the
convenience of being able to pull into any gas station to refuel. It had been a
long project, but it had been great fun.
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